





Advanced Molecular Engineered Lubricants.



FIJI GOVERNMENT DEPARTMENT OF ENERGY

MINISTRY OF PUBLIC UTILITIES [Water & Energy]
DEPARTMENT OF ENERGY
P O Box 2493
Government Buildings Tel : (679) 338 6677, 338 6006
E-
Wednesday 17th June 2009.
To Whom It May Concern,
The Department of Energy is pleased to fully endorse and recommend the BITRON range of products.
After reviewing and witnessing the very practical demonstration of the BITRON products, reviewing recent lab results, reviewing numerous local and international testimonials and testing the Bitron products we are happy to ENDORSE and RECOMMEND the Bitron product range for its ability to:
IMPROVE FUEL EFFICIENCY HENCE REDUCING FUEL & ENERGY USAGE
REDUCE ENGINE WEAR & TEAR
REDUCE CARBON EMMISSIONS BY UP TO 90%
In utilizing Bi-
Vilimone W Vosarogo.
Engineer , Department of Energy.
Ministry of Public Utilities.
Email: vvosarogo@fdoe.gov.fj
ph 3386006 ext 132, mobile 9273983

Consort Shipping
Consort Shipping use 30,000-

Inter Island Barge
Barge fitted with twin 8V7IS Detroit Engines was using 790 litres of diesel on round trip to islands. The engineer decided to trial Bitron over 6 months. To his amazement the fuel usage dropped to 600 litres – a saving of 24%. He used Bitron Diesel Fuel Treatment and EP20 Engine Treatment, along with EP40 Powertrain & Gear Formulation in his Allison transmission. Everything runs smoother and quieter as a result of reduced friction.

Burdekin Transport Queensland Australia
Uses Bitron Diesel Fuel Conditioner, Engine Formulation & EP Metal Treatment
Detroit SER60 450HP engine, has done 1.7 million kilometres. Was using 2½ litres of oil every two weeks, added Engine Formulation and now uses NO oil.



THERE ARE MANY MORE TESTIMONIALS. Contact us to learn more about our customer cost savings

Fuel Tanker Chris Fordham – Jenfor Transport – GARBUTT, Queensland, Australia: Owner
driver of B-
Jenfor use Bitron Diesel Fuel Conditioner, Engine Formulation & EP Metal Treatment.
Stopped adding Diesel Fuel Conditioner, took 8-


Using Bitron Engine Formulation and Diesel Fuel Conditioner in 360HP Cummins-
Initially saved 5% in fuel consumption. With continued use over a two year period,
savings gradually improved through 10%, 15%, 20% and eventually in excess of 30%.
After 30,000 hours Cummins traded-


Truck Diesel Savings John Galea – Johnny Farming Co. – MACKAY, Queensland, Australia
Trialling Diesel Fuel Conditioner over same distance with the same load and drivers, saved 20% on fuel. Now buys all Bitron products (Diesel Fuel Conditioner, Engine Formulation and EP Metal Treatment) and recommends using Engine Formulation in conjunction with Diesel Fuel Conditioner for optimum results.
John also operates a shrimp farm and uses Bitron products in his tractors and other equipment. When an unattended tractor running a stationary pump lost all of its coolant, John was surprised to find the overheated tractor still running when he returned. It is his firm belief that Bitron Lubricants EP20 Engine treatment saved his tractor from the usual damage and likely seizing due to overheating.


Cyril Vale – Owner Mendip Hills Pastoral Company, Jericho QLD
Equipment: Caterpillar 12H Grader;
D6H Dozer;
D85 Komatsu Dozer;
New Caterpillar 12H required scheduled oil sample (SOS) analysis by Hastings Deering
under the terms of the manufacturer’s warranty. As Bi-
In 2007 Bi-
The 3rd and 4th oil samples showed a further reduction in these contaminants and wear factor.
Using the Caterpillar’s computerised fuel flow meters, fuel consumption was shown to be reduced from 16 litres per hour to 14.12 litres per hour – A reduction [in fuel consumption] of 11.75%
Cyril Vale noted improved general performance, notably power and smoothness.
“I would recommend Bi-

|
CONTAMINANT |
BEFORE |
AFTER |
% Reduction |
|
Copper (Cu) |
6 |
2 |
66% |
|
Iron (Fe) |
16 |
8 |
50% |
|
Aluminium (Al) |
4 |
2 |
50% |
|
Soot (ST) |
33 |
28 |
15% |
|
Sulphur (Sul) |
14 |
11 |
21% |

I prepare and race a Suzuki Pro stock drag bike. The engine develops approximately 200BPH at 12,500RPM from only 1200cc. As you can imagine most of the engine parts are put through a lot of stress. The 17:1 static compression ratio is very hard on parts such as gudgeon pins and crankshaft bearings.
The maintenance program on my engine is very time consuming, due to the need of a complete engine rebuild after every race meeting. With constant repair or replacement of parts like gudgeon pins, cams and rockers, engine bearings etc, even a high volume oil pump gear set was not enough to slow the rate of destruction.
I have tried many types of oil additives over the past ten years of racing these
engines, with absolutely no effect on my results. But then I tried Bi-
So being a true drag racer looking for every advantage, I decided to step up the compression ratio to 17.6:1 and fitted standard oil pump gears (high volume gears use an extra 4HP to drive) after all, I may as well test this product to the limits. Again after the next meeting I pulled down the engine and the results were the same. No wear on any parts. The engine didn’t need any maintenance at all.
I have now competed in five race meetings without inspections. If I had been using this product for the last ten years, I would have saved tens of thousands of dollars on worn parts not to mention my time.
Bi-
I now use this product in every motorcycle I work on whether it is for racing or
street use. Every engine will benefit from Bi-
My customers are also impressed with the results they are getting. When something is this good, word travels fast, and my workshop is really going well, and building every day.
Thanks Bi-
B. Lennon. Vic.

The engine driving the 900CFM/350 PSI, 2 stage sullair compressor consumed:
Before Bi-
With this fuel saving Bi-
